Wednesday, March 11, 2009

Return of the Gremlins

Yesterday my car wouldnt start. When i got home from school, it started right up. Today before i headed to the yard it refused to start again. After some fiddling around in the wiring, I found that one of my relays had gone bad.

I went to the yard and picked up a relay and pulled apart aac valves from a couple different cars. After i got home, more tests pointed toward the source power to the fuel pump relay was low and caused it to flicker when it was key on. I changed to a different source wire and it fired right up.

On my way to Justins house, my car gave up. After Jumping it, I drove it into his driveway where he had a look at it for me. Turns out that the alternator decided to let go. Luckily, he had a dual cam ka alternator laying around. The alternator fit with the dual cam ka hardware, some washers, and a modification to the rb upper alternator bracket. Several hours later (after some pizza and a few trips to different stores), it was all back together and running again.

Justin also had an extra aac spring from an sr. I threw it in and now my idle is low. At this point it should only be some timing adjustment and a bit of the idle screw in the back of the manifold.

Tuesday, March 10, 2009

Photos

Here's the most recent photo update. Not much news to add, really. I'm pretty confindent that the problem in the idle lies with the aac valve. Tomorrow i'm going to the yard to see if i can find something.