Sunday, October 18, 2009
Tension back home
Today I put my zccjdm tension rods in. They're nice and sturdy and have plenty of adjustability. I did a quick throwtogether alignment just to have the wheel centered. I will get it actually aligned when I put together the rest of the sus.
Friday, October 2, 2009
Out of Control Speed
Today i replaced the speed sensor cable that broke on me a couple weeks ago. My solid diff mount, transmission crossmember bushings, and zcc tension rods came in. Just waiting for a couple more things to work on the sus.
Between now and the prevous post, i got a pressure reg and dialed in the fuel pressure.
Between now and the prevous post, i got a pressure reg and dialed in the fuel pressure.
Thursday, August 20, 2009
Friday, July 3, 2009
Don't touch the mustache
Today I had the day off so I decided to work on the mustache bar bushings, since its supposed to be a relatively tame install. It wasn't too difficult, just had to undo the bolts to the diff, frame, and a couple other things and it popped off. The old bushings had to be burned out, which was kind of a pain in the summer heat.
Predictably, it's reduced some driveline slop



Predictably, it's reduced some driveline slop



Monday, June 22, 2009
The yard
Today i scored a pair of s12+8 calipers and a rear review mirror that doesnt have a broken flange
Wednesday, March 11, 2009
Return of the Gremlins
Yesterday my car wouldnt start. When i got home from school, it started right up. Today before i headed to the yard it refused to start again. After some fiddling around in the wiring, I found that one of my relays had gone bad.
I went to the yard and picked up a relay and pulled apart aac valves from a couple different cars. After i got home, more tests pointed toward the source power to the fuel pump relay was low and caused it to flicker when it was key on. I changed to a different source wire and it fired right up.
On my way to Justins house, my car gave up. After Jumping it, I drove it into his driveway where he had a look at it for me. Turns out that the alternator decided to let go. Luckily, he had a dual cam ka alternator laying around. The alternator fit with the dual cam ka hardware, some washers, and a modification to the rb upper alternator bracket. Several hours later (after some pizza and a few trips to different stores), it was all back together and running again.
Justin also had an extra aac spring from an sr. I threw it in and now my idle is low. At this point it should only be some timing adjustment and a bit of the idle screw in the back of the manifold.
I went to the yard and picked up a relay and pulled apart aac valves from a couple different cars. After i got home, more tests pointed toward the source power to the fuel pump relay was low and caused it to flicker when it was key on. I changed to a different source wire and it fired right up.
On my way to Justins house, my car gave up. After Jumping it, I drove it into his driveway where he had a look at it for me. Turns out that the alternator decided to let go. Luckily, he had a dual cam ka alternator laying around. The alternator fit with the dual cam ka hardware, some washers, and a modification to the rb upper alternator bracket. Several hours later (after some pizza and a few trips to different stores), it was all back together and running again.
Justin also had an extra aac spring from an sr. I threw it in and now my idle is low. At this point it should only be some timing adjustment and a bit of the idle screw in the back of the manifold.
Tuesday, March 10, 2009
Photos
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